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Got a Harbor freight titanium 125 flux core.wire feeder

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发表于 2021-11-13 15:51:37 | 显示全部楼层 |阅读模式
Picked it up last night.  Have not welded with fluxcore on about 15 yrs.  Thought i might be able to use it instead of stick for outside installs.  Probably could but o have no use for this process.The machine will weld.  Produces great heat for upto 3/16. Took 4 minutes ro set up to weld.  Must of that time was spent feeding the wire.  It has a jog switch inside but that was discovered after I paid attention the instructions.I cannot believe i used to weld with this stuff.  I could not seen the edges of the puddle.  Lots of spatter and residue.  The only issue with the welder is it pisses our occasionally.  I thought if was because my contact tip was to close as it was shorting across spatter, but it happened with a 1 in space.I thought I could use for tacking steel for gang cutting, but nope. TooI will return it tomorrow.  A couple welds.  Veritcal up capping a 6013 bead on 1/8"  used machine setting deom.the panel.The second is a.butt joining 2  1/16" steel tubes.  I could see the puddle but not the edges of puddle.

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Reply:I am not trashing the machine.  It weld well.  I personally have no use no shielded flux core.Only issue i did have was the arc powering tapering/sputtering during welding. At some point during the long weld it would taper off them go back to normal. ???  Those are 6 inch continuous welds.  I did not play with settingLast edited by tapwelder; 18 Hours Ago at 09:45 AM.
Reply:I take it the first use of fluxcore. I do not like 120volt welders But to get the best out of a to 120 volt you need to use E70-GS 0.030 wire. They say you can use other size but does not work well for most welders. Note the Chicago 170 is a 240 volt welder and does work great. Dave

Originally Posted by tapwelder

Picked it up last night.  Have not welded with fluxcore on about 15 yrs.  Thought i might be able to use it instead of stick for outside installs.  Probably could but o have no use for this process.The machine will weld.  Produces great heat for upto 3/16. Took 4 minutes ro set up to weld.  Must of that time was spent feeding the wire.  It has a jog switch inside but that was discovered after I paid attention the instructions.I cannot believe i used to weld with this stuff.  I could not seen the edges of the puddle.  Lots of spatter and residue.  The only issue with the welder is it pisses our occasionally.  I thought if was because my contact tip was to close as it was shorting across spatter, but it happened with a 1 in space.I thought I could use for tacking steel for gang cutting, but nope. TooI will return it tomorrow.  A couple welds.  Veritcal up capping a 6013 bead on 1/8"  used machine setting deom.the panel.The second is a.butt joining 2  1/16" steel tubes.  I could see the puddle but not the edges of puddle.
Reply:

Originally Posted by tapwelder

Picked it up last night.  I will return it tomorrow.  I could see the puddle but not the edges of puddle.
Reply:Thanks.  I will try some lincoln stufff tonight
Reply:Oh my.  Picked a spool of lincoln. Nr211.  What a difference over the roll supplied with the machine.  Thank for the tip.  The dream is still alive...
Reply:I am glad 😊 the welder is working for you.Dave

Originally Posted by tapwelder

Oh my.  Picked a spool of lincoln. Nr211.  What a difference over the roll supplied with the machine.  Thank for the tip.  The dream is still alive...
Reply:

Originally Posted by tapwelder

Oh my.  Picked a spool of lincoln. Nr211.  What a difference over the roll supplied with the machine.  Thank for the tip.  The dream is still alive...
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